September-October 2007

Underground Safety

Canal upgrading boosts efficient water use and promotes safety by moving water from an open concrete bed to HPDE 3-feet underground.

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By Lynn Tilton

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“We had to dig 3 feet below the old canal, which was 6.5 feet below grade. The old canal was 8 feet wide at the bottom and 20 feet wide at the top. After we put the pipe in place and fused to the newly installed segments, we did a vision inspection of each seam before covering the pipe.”

But what about dealing with the road crossings? After noting his company also had 21 utilities to deal with, Stratton comments that by working with an excavator on each side of a bridge, crews were able to remove the concrete and dig a trench at the right depth. After that, it was a matter of pulling fused segments of the pipe underneath each bridge so there was 50 feet of exposed pipe on each side of a bridge. This strategy made it easier to fuse those segments to the approaching line.

“We’ve been using HDPE for seven to eight years, but never any this large. Up to that time, the biggest HDPE we had installed was 30 inches. We rented a machine large enough to fuse the segments. There are a limiter number of machines that can handle pipe with such large diameters. Plus, with such a machine costing about $400,000, it made sense to rent instead of buying. We have our own smaller machine, which can handle 24-inch tubes.”

Stratton, who has been dealing with construction for 25 years, emphasizes his company used all the construction windows each year to ensure timely completion. “We have a crew that does the outlets; another crew builds boxes for concrete gate valves. It was a straightforward construction project. The only problem we had was during the second year when some material for the outlets didn’t arrive on time.” But material supply wasn’t a problem during the third phase because some of the products were onsite a week before the end of the second phase. Again, timely delivery kept the project on the go and offered a timely disposal of funds, which is another money saver.

Stratton comments that weekly meetings with the Water Conservation District year-round helped to make the project easier to complete. He emphasizes advance orders of outlets and flow valves avoided a repetition of the problem during the final phase.

Keeping Neighbors Happy
A common chore for all elements of the St. George and Washington Fields canal project was keeping the neighbors happy, especially during construction. Stratton comments, “We met with property owners to explain our schedule for working near their homes or farms, and exactly what we were going to be doing. Since safety issues were being addressed, most people were happy to see the canal go into the pipeline. Basically, our contract called for installing the pipe with different outlets for secondary rural residential use. Both Washington City and St. George have future outlets planned so as the cities grow they can plan to pipe water into those areas.”

With 150 to 300 employees in this branch of Interstate Rock Products, the company has placed all kinds of other pipe, but the 63-inch and 54-inch HPDE was the largest it’d ever dealt with. “We really enjoyed this project because it had good working conditions and good coordination with the engineering company, owners, and residents. People along the route were satisfied because we kept moving along the canal. Neighbors don’t like construction sites to last a long time. We also kept out of people’s front yards.”

Crag Stratton notes Interstate has been in business since the late 1950s and has always tried to maintain a working relationship with all involved in a given project. “We work hard to get the job done. It’s a win-win situation.”

Meanwhile, Back to the WSD
Looking back on the St. George and Washington Fields canal project, Ron Thompson comments, “This project was particularly remarkable because it required a lot of people working together. Thanks to everyone involved, the project went smoothly, and has saved a lot of water. That savings can be used to help both cities improve their parks’ turf and there will be more secondary water available as the population continues to increase. At the same time water availability to farmers using the canal will be more consistent.”

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What about the small reservoir serving the canal? Thompson responds, “A regular reservoir is on the agenda at the head of the canal. It will hold 25,000 to 30,000 acre-feet, and has the capacity to ensure even more water during dry times. Naturally, the reservoir will make room for other distribution systems without compromising water delivery through the St. George and Washington Fields canal.”

Ron Thompson, along with everyone else involved in piping the canal, is pleased that the project saves about 4,400 acre-feet. Again, this savings means greater use of cleaner secondary water. And a substantial share of that savings means greater utilization of culinary water.

Author's Bio: Lynn Tilton is a frequent contributor to Forester Communications publications.

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