September-October 2007

Underground Safety

Canal upgrading boosts efficient water use and promotes safety by moving water from an open concrete bed to HPDE 3-feet underground.

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By Lynn Tilton

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Besides providing cleaner water, burying the pipe makes it possible to use the canal easement for a maintenance road or trail. Best of all, the buried pipe removed safety concerns.

When Alpha got the contract in July 2004, it had to have the design completed that November. “We also had to prepare a list of materials for the canal company, and they took it from there. The first phase of the three-year project ran from December 1, 2004, until March 1 2005, and saw a mile of pipe installed. Basically, the contractor, Interstate Rock Products in nearby Hurricane, Utah, removed and pulverized the concrete, which they mixed with backfill material. Their trenching was deep enough to allow 3 feet of cover over the HDPE pipe.”

Another challenge was to find HDPE with the massive diameter called for. JM Eagle of Livingston, NJ, the largest manufacturer of HDPE and PVC piping in the world, supplied the solution. With 14 plants in the US alone, the nearest one, located about 200 miles south in Kingman, AZ, took on the challenge to manufacture the first 63-inch pipe in the nation.

As the project continued, Alpha reps attended weekly meetings with the conservancy district and canal officials. Gardner’s people also were onsite to help with any unexpected situations. “We had up to five people involved with the project during the design and construction periods. Because of the long growing season, time was a limitation. We also had several other ongoing projects we were working on at the same time and had to be efficient to get this project done in a timely manner. We are in a relatively small community so we need people with all kinds of skills, people who can do everything connected with civil engineering.”

Coordinating the Project
With timeliness and avoiding cost overruns two essential elements, a key player in a project is the program coordinator. In this case, Doug Wilson, special project coordinator for the Washington County Water Conservancy District, was given that responsibility. He says, “The district covers the whole county and we are one of the largest shareholders in the canal company. Before I got the assignment to coordinate the construction, the project was pretty well thought out. My main responsibility during the construction phases was to keep everybody on the go.”

Coordination with all parties involved in the project was essential because there wasn’t much time each year to spend replacing the old open canal. “We have a long growing season with acres of corn, alfalfa, and other such crops relying on the canal for their water supply.” He adds that because of the high mineral content, there are no commercial orchards on the acreage served by the canal.

A plus for the canal is the mild winters. Snow is rare, happening perhaps once a winter. Ice is not a problem with the open canal. Now that it’s 3 feet underground, it’s well insulated. This further helps ensure better longevity for the buried canal, making the investment even more sensible.

“The canal runs west, then south and west again. High land values are prompting farmers to sell their acreage for residential construction. The canal used to supply water strictly for agriculture, but now it’s used as secondary water in residential lots. It’s also used for recreational use where turf is important. For example, some golf courses rely on the canal for water.”

Like Gardner, Wilson sees the project as a means for making better use of water than possible when exposed to evaporation—and seepage. Some estimates report that as much as 10% of the water in the concrete canal was lost to seepage. Eventually, seepage led to washouts. “By piping the canal, those problems are behind us. It has cut down on the maintenance workload because the canal doesn’t have to be cleaned every year like it used to.”

Another natural challenge of seepage and open ditches was that those at the end of the canal got less water than those at the head. Water delivery is timed, rather than measured. So the more flow water users get for the time allowed, the more they can utilize it.         

Wilson, who has been dealing with water issues for 10 years, comments the full length of the canal goes through the Moenkopi formation of rock and clay, interlaced with gypsum. This combination of soil caused settlement in parts of the canal, which led to cracks, which led to washouts in some places. The company first used liners in the troubled areas. But even the liners proved merely to be a temporary fix.

He adds that the low grade of the canal slowed water flow, causing sediment to drop and settle on the bottom of the canal. Naturally, this decreased the capacity of the canal. “We’ve had no silt dropout since we put in the silt and sediment control devices to make for cleaner water before it entered the pipe.”

Photo: Washington County Water Conservancy District
The canal supplies water for agriculture and secondary water in residential lots.

Wilson emphasizes that keeping the project on time and within budget took a lot of work in planning, design, and coordination of the elements that make up a complicated project.

One complication involved the roads the canal crossed under. “Fortunately there were just five of those, with only one paved road in the entire length. When the contractor came to those, his people trenched under the roads from both sides and pulled the HPDE pipe through. This avoided any problems with traffic.”

He says, “The public reaction has been positive for the city because there’s more water available for city recreation use. The concrete canal had a 25-foot right of way on each side. By placing the canal underground, that level ground is becoming more and more popular for recreational use.”

Timely Construction
After the canal company got the materials list from Alpha, it put the construction portion out for bid. Interstate Rock Products, which has a branch southeast of St. George in Hurricane, proved to be the low bidder. “We prepared the ground and put 5,000 feet of 63-inch pipe the first winter, 30,000 the second winter, and 13,000 feet of 54-inch pipe in the third season,” says Craig Stratton, secretary-treasurer for the corporation.

Advance material ordering helped Interstate meet the timeline demands. “We couldn’t shut off the canal until the first of December and had to have the flow back in place the first of March. With 15 to 25 employees on the site we were able to get a lot done even with such a short work window.”

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One element that helped was ordering the 63-inch from local supplier Isco Industries in West Jordan, UT, a month prior to use. Stratton adds, “The pipe came in 50-foot lengths. We fused 10 to 15 pipes together above ground and then placed the completed sections in the trench. We used a portable crusher to deal with the concrete, and saved it to mix with the soil brought in to use for overburden.”

He says this move made it possible to fill 20% of the overburden needs. Sourcing soil for fill ranged from 3 miles to 10 miles. The portable crusher moved along the canal as workers dumped crushed concrete in the hopper. This reduced the time needed to get fill material onsite, which reduced the cost of installation. Next Page >

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